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    <title>Kinetis Motor Suite中的主题 Re: Motor Measure issue in position control</title>
    <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733053#M388</link>
    <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;Did you attempt the resolution steps in the message?&amp;nbsp;&amp;nbsp;Since the LINIX motor does not have a rear shaft, you may need to switch the A &amp;amp; B phases of the encoder so that the motor and encoder are aligned to the same direction.&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
    <pubDate>Mon, 16 Apr 2018 14:17:37 GMT</pubDate>
    <dc:creator>linestream-adam</dc:creator>
    <dc:date>2018-04-16T14:17:37Z</dc:date>
    <item>
      <title>Motor Measure issue in position control</title>
      <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733052#M387</link>
      <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;Dear,&lt;/P&gt;&lt;P&gt;&amp;nbsp; &amp;nbsp; &amp;nbsp; &amp;nbsp;When i start a position with LINIX-45ZWN24-40 BLDC motor(24V, 2P, 4000R/M) and EB38S6A-1000-3L G2 Encoder, i found a problem in motor measure step as below. Could you tell me how to resolve this probelm.&lt;/P&gt;&lt;P&gt;&amp;nbsp; &amp;nbsp; &amp;nbsp; &amp;nbsp;&lt;span class="lia-inline-image-display-wrapper" image-alt="PMSM_Position_measure_motor_issue.PNG"&gt;&lt;img src="https://community.nxp.com/t5/image/serverpage/image-id/8195i8F1B1B9AD234129E/image-size/large?v=v2&amp;amp;px=999" role="button" title="PMSM_Position_measure_motor_issue.PNG" alt="PMSM_Position_measure_motor_issue.PNG" /&gt;&lt;/span&gt;&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
      <pubDate>Sun, 15 Apr 2018 15:34:53 GMT</pubDate>
      <guid>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733052#M387</guid>
      <dc:creator>bansondou</dc:creator>
      <dc:date>2018-04-15T15:34:53Z</dc:date>
    </item>
    <item>
      <title>Re: Motor Measure issue in position control</title>
      <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733053#M388</link>
      <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;Did you attempt the resolution steps in the message?&amp;nbsp;&amp;nbsp;Since the LINIX motor does not have a rear shaft, you may need to switch the A &amp;amp; B phases of the encoder so that the motor and encoder are aligned to the same direction.&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
      <pubDate>Mon, 16 Apr 2018 14:17:37 GMT</pubDate>
      <guid>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733053#M388</guid>
      <dc:creator>linestream-adam</dc:creator>
      <dc:date>2018-04-16T14:17:37Z</dc:date>
    </item>
    <item>
      <title>Re: Motor Measure issue in position control</title>
      <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733054#M389</link>
      <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;I have tried all scenarios (total 6 kinds connection type), but failed. Does the LINIX motor can not be used to position control?&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
      <pubDate>Mon, 16 Apr 2018 15:11:03 GMT</pubDate>
      <guid>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733054#M389</guid>
      <dc:creator>bansondou</dc:creator>
      <dc:date>2018-04-16T15:11:03Z</dc:date>
    </item>
    <item>
      <title>Re: Motor Measure issue in position control</title>
      <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733055#M390</link>
      <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;I've used the linix motor with position control successfully using an encoder.&amp;nbsp;&lt;/P&gt;&lt;P&gt;&lt;/P&gt;&lt;P&gt;What number are you putting in to Encoder Lines?&amp;nbsp; This value should be the number of lines on the encoder wheel and not the maximum count.&amp;nbsp; I've been unable to find a datasheet for your encoder to know if the 1000 refers to number of lines or to maximum count.&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
      <pubDate>Mon, 16 Apr 2018 15:39:42 GMT</pubDate>
      <guid>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733055#M390</guid>
      <dc:creator>linestream-adam</dc:creator>
      <dc:date>2018-04-16T15:39:42Z</dc:date>
    </item>
    <item>
      <title>Re: Motor Measure issue in position control</title>
      <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733056#M391</link>
      <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;Hello, Mr. Reynolds. I put in 1000 to Encoder Lines which be marked in encoder's nameplate. You can find the below picture. Could you please give me some suggestion how to do. Thank you~&lt;/P&gt;&lt;P&gt;&lt;span class="lia-inline-image-display-wrapper" image-alt="encoder.jpg"&gt;&lt;img src="https://community.nxp.com/t5/image/serverpage/image-id/11431i3ACAFF3AD99C11A6/image-size/large?v=v2&amp;amp;px=999" role="button" title="encoder.jpg" alt="encoder.jpg" /&gt;&lt;/span&gt;&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
      <pubDate>Mon, 16 Apr 2018 16:12:14 GMT</pubDate>
      <guid>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733056#M391</guid>
      <dc:creator>bansondou</dc:creator>
      <dc:date>2018-04-16T16:12:14Z</dc:date>
    </item>
    <item>
      <title>Re: Motor Measure issue in position control</title>
      <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733057#M392</link>
      <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;You can try putting 250 for the number of encoder lines.&lt;/P&gt;&lt;P&gt;&lt;/P&gt;&lt;P&gt;Next resolution steps would be to switch to Motor Manager, and navigate to the Position Control tab.&amp;nbsp; Manually rotate the motor shaft anti-clockwise (when looking at the face of the motor) and ensure that you are getting positive numbers in Position Feedback.&amp;nbsp; If you are getting negative numbers, switch the A &amp;amp; B phases of the encoder.&amp;nbsp; If you are getting&amp;nbsp;0,, verify the wiring of your encoder since the MCU is not able to see the encoder pulses.&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
      <pubDate>Mon, 16 Apr 2018 17:34:09 GMT</pubDate>
      <guid>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733057#M392</guid>
      <dc:creator>linestream-adam</dc:creator>
      <dc:date>2018-04-16T17:34:09Z</dc:date>
    </item>
    <item>
      <title>Re: Motor Measure issue in position control</title>
      <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733058#M393</link>
      <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;Hello, Mr. Adam Reynolds:&lt;/P&gt;&lt;P&gt;&amp;nbsp; &amp;nbsp; &amp;nbsp; &amp;nbsp; &amp;nbsp; I have changed encoder lines from 1000 to 250. But problem is still occured. I used LINIX-45ZWN24-40 motor which is 2 poles motor. My question is that is it can used into position control? &amp;nbsp;And how to switch to motor manager? Thank you~&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
      <pubDate>Sat, 21 Apr 2018 09:44:45 GMT</pubDate>
      <guid>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733058#M393</guid>
      <dc:creator>bansondou</dc:creator>
      <dc:date>2018-04-21T09:44:45Z</dc:date>
    </item>
    <item>
      <title>Re: Motor Measure issue in position control</title>
      <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733059#M394</link>
      <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;Yes, I've used the Linix motor for position controller successfully many times.&amp;nbsp; The issues you are running into&amp;nbsp;are related to the wiring of the encoder and/or motor.&amp;nbsp; When running in position control it is important that the direction or rotation is aligned for the encoder and the motor.&lt;/P&gt;&lt;P&gt;&lt;/P&gt;&lt;P&gt;You can switch to Motor Manager by clicking the&amp;nbsp;&lt;span class="lia-inline-image-display-wrapper" image-alt="2018-04-23 07_53_51-Kinetis Motor Suite_ C__Work_420maFRDM_Freescale_ARM_iar_frdmkv31fInTAC_ProjectT.png"&gt;&lt;img src="https://community.nxp.com/t5/image/serverpage/image-id/47371i39E69A09454CBD85/image-size/large?v=v2&amp;amp;px=999" role="button" title="2018-04-23 07_53_51-Kinetis Motor Suite_ C__Work_420maFRDM_Freescale_ARM_iar_frdmkv31fInTAC_ProjectT.png" alt="2018-04-23 07_53_51-Kinetis Motor Suite_ C__Work_420maFRDM_Freescale_ARM_iar_frdmkv31fInTAC_ProjectT.png" /&gt;&lt;/span&gt;&amp;nbsp;button.&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
      <pubDate>Mon, 23 Apr 2018 11:57:11 GMT</pubDate>
      <guid>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733059#M394</guid>
      <dc:creator>linestream-adam</dc:creator>
      <dc:date>2018-04-23T11:57:11Z</dc:date>
    </item>
    <item>
      <title>Re: Motor Measure issue in position control</title>
      <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733060#M395</link>
      <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;What step did you get this error in?&lt;/P&gt;&lt;P&gt;I got this error too while tuning my motor in the "Automatic Parameter Measurement" step.&amp;nbsp; I was tuning with a rotor attached that had a high inertia.&amp;nbsp; The way I fixed it was to reduce the "Flux Identification Speed" % gradually until it quit getting the error and it passed.&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
      <pubDate>Tue, 24 Apr 2018 12:58:00 GMT</pubDate>
      <guid>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733060#M395</guid>
      <dc:creator>randyfields</dc:creator>
      <dc:date>2018-04-24T12:58:00Z</dc:date>
    </item>
    <item>
      <title>Re: Motor Measure issue in position control</title>
      <link>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733061#M396</link>
      <description>&lt;HTML&gt;&lt;HEAD&gt;&lt;/HEAD&gt;&lt;BODY&gt;&lt;P&gt;Randy, great point.&amp;nbsp; Couple of things to note here.&amp;nbsp; This error can only occur when performing the flux identification as that step requires rotating the motor.&amp;nbsp; Additionally, that is why it is important that the motor be as disconnected from any load or inertia when performing this tuning.&amp;nbsp; In order to get an accurate identification, we need to be sure that the motor can freely spin.&lt;/P&gt;&lt;/BODY&gt;&lt;/HTML&gt;</description>
      <pubDate>Tue, 24 Apr 2018 13:59:38 GMT</pubDate>
      <guid>https://community.nxp.com/t5/Kinetis-Motor-Suite/Motor-Measure-issue-in-position-control/m-p/733061#M396</guid>
      <dc:creator>linestream-adam</dc:creator>
      <dc:date>2018-04-24T13:59:38Z</dc:date>
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